- Open Access
- Total Downloads : 562
- Authors : Azam Khan, Mian Tauseef Raza
- Paper ID : IJERTV4IS060548
- Volume & Issue : Volume 04, Issue 06 (June 2015)
- Published (First Online): 19-06-2015
- ISSN (Online) : 2278-0181
- Publisher Name : IJERT
- License: This work is licensed under a Creative Commons Attribution 4.0 International License
Coiled Tubing Acidizing: An Innovative Well Intervention for Production Optimization
Azam Khan
Department of Petroleum and Gas Engineering University of Engineering & Technology, Lahore Lahore, Pakistan
Mian Tauseef Raza
eni Pakistan, Drilling & Well Operations eni Pakistan, Karachi, Pakistan
AbstractIn the Oilfield Services, Coiled Tubing (CT) is considered as one of the most adaptable and flexible technology. Since its introduction, some forty years ago, Coiled Tubing has aggressively evolved in oil and gas industry. Liquid unloading of the wells and sand clean out were the early applications of the Coiled Tubing. Now-a-days, CT is very frequently used in different well interventions, perforating the well and above all the recent developments of the Coiled Tubing Drilling. A lot of other services employed in the past but they showed decline, while CT has shown a growing rate of 10% per year. The speed and convenience of Coiled Tubing has been used to provide benefit to well productivity in different applications. Some common applications of CT are the fracturing, well testing, unloading of the well, acidizing, scale milling and other intervention activities. Today, engineers can change the toughest well into a profitable production well by using the speed and convenience of the CT, strong engineering planning, creative integration and other complementary equipment. In this paper only one application of CT is considered i.e. acidizing. The main purpose of this project was to increase the deliverability of a gas reservoir in which gas production has been reduced due to near well bore damage (skin). The case study is performed for such a well in which production is impaired by skin & reservoir rock is carbonate. The skin value is determined through well testing. The production data before acidizing & well testing has confirmed a high value of skin. Inflow performance relationship at current value of skin is plotted. This plot shows that the production is not up to the mark. To make it economical as well as favorable, stimulation has been performed to reduce the skin. By reducing the skin a considerable increase in production is observed. The entire work has been done on MS Excel. This technique results enhanced productivity of well accelerating hydrocarbons recovery & adding them to the reserves.
KeywordsCoiled Tubing, Matrix Acidizing, Fold of Increase, Skin, IPR, Productivity Index, Absolute Open Flow Potential
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INTRODUCTION
Coiled tubing was developed in 1944 to serve as a continuous fluid carrying pipeline under the oceans. After world war (II) it starts to be considered for applicability in petroleum industry. The first trial was made by Bowen Tools and Brown Oil Tools, their continuous efforts resulted in evolution in CT development and they started employing it as a well services tool in 1960s and 1970s. Till then it is working as the main component in performing the work over operations and other services of the well.
With time, evolution was continued and CT is gaining widespread popularity in well completion and drilling
operations as well. Major factors in rapid developments in CT were the flexibility, continuous, and both the fluid injection capacity as well as tools conveying ability. Most of the time, operator desires to perform any workovers without killing the well that can be achieved by coiled tubing. To carry out the well intervention without killing a well, three developments in CT were needed, these were
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A continuous conduit that can be pushed into the production string (CT string)
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During job execution, the running and pulling of the string into the well under the pressure (injector head
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The equipment that provides the dynamic seal around the string during the performance of job (stripper or pack off device)
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ADVANRAGES OF COILED TUBING
High speed of running in of hole and pulling out of hole saves time and money, both. It can carry the downhole tools as well as fluid pumping is also possible. These are its major benefits. Also it has small size of unit with very less rig up and rig down time as compared to any fluid injecting equipment. Some of the benefits of CT employment are [1]:
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Safe and efficient procedures for well intervention (live)
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Less well site preparation is needed
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Easy to mobilize and rig-up
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During RIH/POOH circulation can be continued
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Reduction in downtime of production because of less trip time
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Reduced environmental impacts as compared to the conventional methods and less risks associated
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Less number of working crew or personnel are needed
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Lowered costs
Now a day, CT applications, at least, use one of the following sorts;
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The primary and secondary well control systems (stripper and BOP) enables the safe live well intervention i.e. Live Well Operations
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It could be a High Pressure Conduit as it is high strength and rigid, so it provides a conduit for pressurized fluid movements into the wellbore or the way out. This pressure can further be used to operate the hydraulically operated tools that are powered by the movement of pumped fluid
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Fluids can be pumped through the Coiled Tubing without any break, even during the running in of the hole as well as pulling out of the hole i.e. Continuous Circulation
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It is rigid, high strength and flexible at the same time. These qualities enable it to convey the devices and tools in horizontal wells and severely deviated wells i.e. Rigidity and Strength
Coiled tubing has a range of applications and versatile in operations at different locations[3] and wells of diverse and dynamic conditions. It makes difficult to assign standards for equipment and configurations.
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MAJOR COMPONENTS OF COILED TUBING
The control cabin, power pack, injector head, coiled tubing reel, and pressure control equipment are major components of a coiled tubing unit. Power pack is the energy source for the
usually used as 10,000 psi and H2S resistant Quad or Combi. They are operated by accumulator and hydraulic circuit in the control cabin. A typical Quad BOP consists of the pipe rams, slip rams, shear rams, blind rams, equalizing valves, upper and lower connection ends, a side port and a pressure port. Combi BOP have combined, single ram set of both, the blind ram and shear ram.
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CASE STUDY
A well was drilled in a carbonate reservoir and producing less than the anticipated and it was shown from well test that there was some skin. Through well testing, it comes to know that the initial value of skin was 40. At this value of skin, IPR of reservoir has been plotted in which wellbore flowing pressure has been decreased from reservoir pressure to atmospheric pressure to calculate the absolute open flow potential of the well (see Fig. 1). The well data is shown in table 1. To calculate the mentioned properties of reservoir fluid, KAYs correlation in graphical form was employed. Its results are shown in table 2. By using the pseudo steady state equation for gas flow rate[4],
kh( pR 2 pwf 2 )
whole equipment and processes. It provides hydraulic energy for the operation and functioning of CT unit. It further contains diesel engines to drive the hydraulic pumps to
qsc
1422T g z(ln
re rw
3 S ) 4
provide every component with required pressure energy and the desired flow rate. Control cabin is the control room of CT unit. It contains the clutches, gears and rest of the stuff to observe and control the performance of the job. CT string is spooled onto the coiled tubing reel. It makes the storage and transportation of CT string a lot easier. When the CT is injected into the well, energy is provided by the injector head and same is the case with retrieving back. For the smooth feeding of CT to well and proper spooling onto the reel, a tension is needed in the string. Injector head consists of two oppositely driven endless chains. Gripper blocks, tubing outer diameter size series of grippers, are mounted on the chains for improved grip. Tubing is held in between the oppositely pressed chains. This arrangement is responsible for carrying the total weight of the CT string in the wellbore. To run or retrieve the tubing, hydraulic motors are used to drive the chains. Stripper and BOP stack come under the heading of pressure control equipment.
Stripper ensures a pressure seal in dynamic string environment that is, during run in and pull out. It is hydraulically operated and controlled from the control cabin. There is a packer in the stripper with inserts that are forced to seal against the tubing string. While the BOP stack consists of Quad and Combi BOPs. They are secondary pressure barrier,
The calculations of qsc for skin 40 are given in the table
below. The calculations show that, flow rate is not up to the mark. AOFP for this value of skin is 2.61 MMscf/D. The graph is shown in Fig. 1.
Table 1
Average reservoir pressure
PR
2200 psia
Reservoir net thickness
H
26.5 ft
Permeability of the formation
k
15.5 mD
Reservoir temperature
T
180 0F
Initial value of skin
s
40
Specific gravity of gas
g
0.64
Radius of well bore
rw
0.3266 ft
Drainage radius
re
2000 ft
Table 2
Compressibility Factor
z
0.88
Viscosity
µg
0.0201 cp
Table 3
Pressure (psig)
Flow Rate (MMSCFD)
pR
pwf
s=40
s=30
s=20
s=10
s=5
s=0
s=-1
2200
2200
0
0
0
0
0
0
0
2200
2100
0.230
0.291
0.395
0.614
0.850
1.383
1.580
2200
2000
0.450
0.568
0.771
1.200
1.662
2.701
3.088
2200
1900
0.659
0.832
1.129
1.757
2.434
3.956
4.522
2200
1800
0.857
1.083
1.469
2.286
3.166
5.147
5.884
2200
1700
1.045
1.320
1.791
2.787
3.859
6.275
7.172
2200
1600
1.222
1.543
2.095
3.259
4.513
7.338
8.388
2200
1500
1.389
1.753
2.380
3.703
5.128
8.337
9.530
2200
1400
1.544
1.950
2.647
4.118
5.704
9.273
10.599
2200
1300
1.690
2.134
2.896
4.506
6.240
10.144
11.596
2200
1200
1.824
2.303
3.126
4.864
6.737
10.952
12.519
2200
1100
1.948
2.460
3.339
5.195
7.194
11.696
13.369
2200
1000
2.061
2.603
3.533
5.497
7.612
12.376
14.147
2200
900
2.164
2.733
3.709
5.770
7.991
12.992
14.851
2200
800
2.256
2.849
3.866
6.016
8.331
13.545
15.482
2200
700
2.337
2.951
4.006
6.233
8.632
14.033
16.041
2200
600
2.408
3.041
4.127
6.421
8.893
14.458
16.526
2200
500
2.468
3.117
4.230
6.581
9.115
14.818
16.938
2200
400
2.518
3.179
4.315
6.713
9.297
15.115
17.278
2200
300
2.556
3.228
4.381
6.817
9.440
15.348
17.544
2200
200
2.585
3.264
4.430
6.892
9.544
15.517
17.737
2200
100
2.602
3.286
4.460
6.938
9.609
15.622
17.857
2200
0
2.609
3.294
4.471
6.957
9.635
15.664
17.905
Skin
Initial AOF
Final AOF
FOI
40
2.61
2.61
1
30
2.61
3.29
1.26274
20
2.61
4.47
1.71388
10
2.61
6.96
2.66656
5
2.61
9.63
3.69295
0
2.61
15.66
6.00393
-1
2.61
17.90
6.86286
Table 4
The calculations for these values of skin are given in table below. After this IPR plot of th well has been plotted to show the increase in well deliverability. The calculations are shown in Table-3.
The IPR plot for different values of skin at same wellbore flowing pressure is shown below in Fig. 2.
As the flow rate from this graph is highly uneconomical, so it was decided to stimulate it to reduce the skin from 40 to 30 and then to 20, 10, 05, 0 and -1 using coiled tubing matrix acidizing. Skin -1 indicates an ideal case when the stimulation job has been done 100% successful.
Figure 1
Figure 2
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RESULTS
A skin of -1 was aimed by acidizing job. The trend of FOI vs. skin removed is shown in a plot between skin vs. FOI in Fig. 3 that helps in operational preparations and target skin value. Our purpose is highlighting the successful results of the acidizing job, not the operational execution. Job was executed and fold of increase (FOI) in production was observed to be
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after achieving skin less than zero. After the successful
acidizing job, the increase in productivity has been calculated by using the relation[2] Where
Ja= productivity index after stimulation Jb = productivity index before stimulation
The graph in Fig. 4 shows that with increasing removal of skin, FOI increases. At skin removed=40, there is maximum FOI, which is an ideal case representing the 100% successful job of acidizing.
Figure 3
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CONCLUSIONS AND RECOMENDATIONS
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In carbonate reservoirs, matrix stimulation can prove very handy for productivity improvement and permeability impairment.
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Stimulation is a cure to damaged wells, but once it is performed successfully it is recommended that link the matrix acidizing with the long term development plans.
REFERENCES
-
R.L. Thomas and A. Milne, The Use Of Coiled Tubing During Matrix Acidizing Of Carbonate Reservoirs SPE 29266.
-
Zerhboub, M., Touboul, E., Ben-Naceur, K., and Thomas, R.L, Matrix Acidizing:A Novel Approach to Foam Diversion SPE 22854
-
Al Ghulam, J., Al Shidi, S., Mazarett, P. Makarem, A Recipe for Testing the Limits in Central Oman Gas Exploration, SPE 68138
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John Lee, Well Testing, 2002.