- Open Access
- Total Downloads : 305
- Authors : Sharanakumar, Dr. Chethan Kumar C S, S. Appaiah
- Paper ID : IJERTV4IS041417
- Volume & Issue : Volume 04, Issue 04 (April 2015)
- DOI : http://dx.doi.org/10.17577/IJERTV4IS041417
- Published (First Online): 30-04-2015
- ISSN (Online) : 2278-0181
- Publisher Name : IJERT
- License: This work is licensed under a Creative Commons Attribution 4.0 International License
Improving the Efficiency of Steam Turbine Rotor Manufacturing
Sharanakumar1
-
ech student, Department of IEM M S Ramaiah Institute of Technology Bangalore, India
Dr. Chethan Kumar C S2, S. Appaiap
Professor2, 3, Department of IEM M S Ramaiah Institute of Technology
Bangalore, India
AbstractThe project was carried out at a reputed steam turbine rotor manufacturing unit, Bangalore. The product considered is steam turbine rotor used for generating power in sugar plant, it is a job order production. Previously, when this rotor was manufactured, the company was not able to supply the product to the customer at the promised time. The customer was not satisfied with this and demanded that the rotor be supplied in time. The cause for this was that the time required to manufacture this particular rotor was 7207 minutes which is quite high. The objective of this project is to reduce the cycle time of the steam turbine rotor manufacturing. The operations involved in steam turbine rotor manufacturing were noted and data was collected for each operation. The operations were classified into value added and non-value added activities and critical examination was applied to non-value added activities that took place on the CNC machine. The non-value added activities that were identified were approach checking, checking dimension values, inspection and chip cleaning. By the application of critical examination, the non-value added activity time was reduced from 1669 minutes to an estimated time of 635 minutes. Single Minute Exchange of Dies technique was applied for the three set up operations. The activities involved in the set up operations were divided into internal and external activities, reducing external and internal activities and then streamlining the internal activities. By doing so the set up operation time was reduced from 2280 minutes to an estimated time of 2140 minutes. By the application of critical examination and single minute exchange of dies technique, the cycle time to manufacture the steam turbine rotor is reduced from 7207 minutes to 6033 minutes. The estimated savings because of the cycle time reduction is found to be Rs. 1, 17,400/-.
Keywords Cycle Time, Value Added Activities, Non Value Added Activities, SMED, Internal Activities, External Activities, Setup time.
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INTRODUCTION
Method study is the technique of systematic recording and critical examination of existing and proposed ways of doing work and developing an easier and economical method [7] [8]. Method study is essentially used for finding better ways of doing work. It is a technique for cost reduction [9]. The philosophy of method study is that 'there is always a better way of doing a job' and the tools of method study are designed to systematically arrive at this better way of doing a job [12]. This procedure involves seven basic steps as follows [10]:
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Select the work to be studied.
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Record all facts about the method by direct observation.
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Examine the above facts critically.
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Develop the most efficient and economic method.
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Define the new method.
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Install the new method
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Maintain the new method by regular checking
Single Minute Exchange of Die (SMED) is one of the many lean production methods for reducing waste in a manufacturing process [3]. It provides a rapid and efficient way of converting a manufacturing process from running the current product to running the next product [1]. This rapid changeover is key to reducing production lot sizes and thereby improving flow [11]. The phrase "single minute" does not mean that all changeovers and startups should take only one minute, but that they should take less than 10 minutes (in other words, "single-digit minute")[2]. Closely associated is a yet more difficult concept, One-Touch Exchange of Die, (OTED), which says changeovers can and should take less than 100 seconds.
-
-
OBJECTIVES
Productivity improvement by reducing the cycle time for Rotor manufacturing.
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METHODOLOGY
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Selection of study to be carried out i.e., manufacturing of turbine rotor
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First the entire processes during manufacturing of turbine rotor are recorded.
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Identified Value added activities and Non Value added activities.
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Total time taken for these above activities is recorded.
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Critical Examination is done on Non value Added activities using Questioning technique
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To reduce the setup time SMED technique is applied
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Setup operations are recorded and analyzed.
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Operations are divided into smaller elements and time taken for each element is noted.
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Identify the internal and external element
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Convert from internal steps into external steps
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Reduce time consumed by the internal steps
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Streamline the new process.
-
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EXISTING METHOD
After recording the timings of all the operations the following observations were done.
Setup time in min
Machining time in min
Non-value added time in min
Total time in min
2280
3258
1669
7207
Table 1: Components of Total time
The non-value added activities time had the following components: approach checking, checking dimension values, inspection and chip cleaning.
Approach checking time In min
Inspection time In min
Checking Dimension values In min
Chip cleaning time In min
378
213
408
670
Table 2: Components of Total time
Present method time:
Setup time = 2280 min
Total Actual cutting time in min = 3258 min Total non value added time in min = 1669 min Total time = 7207 min
Total time in hrs = 120 hr 6 min
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PROPOSED METHOD
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Critical Examination by Questioning Technique
Develop For checking program dimensions values
Before running the program, the operator has to check the dimension values with the data sheet. To avoid this, check list has been developed. By doing so we can eliminate or reduce this time. Before keying the programs to the machine, programmer has to cross check the dimension values in the program. Then inspector in the programming department has to recheck the program and it has to be approved by the programming department. Later it has to be sent to the production department for the process.
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Purpose What should be done?
Provide the check list to reduce checking dimension values time.
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Place Where should it be done?
It should be done at the programming department
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Sequence When should it be done?
Soon after preparing the programs and before keying it into the machine
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Person Who should do it? Programming dept should do it.
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Means How should it be done?
It should be done using process sheet.
For approach checking
This can be avoided by providing the checklist for the programming department. The programmer can cross check the program after developing the program. The same should be approved by the programming department. This reduces the operators time to check the program.
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Purpose What should be done?>
Provide the check list to reduce approach checking.
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Place Where should it be done?
It should be done by the programming department
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Sequence When should it be done?
After preparing the programs by the programmer
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Person Who should do it?
Programming department should do it.
Check list for Checking Dimension values and Tool approach checking during programming
The checklist was prepared after discussion with the production engineer, supervisor, programmer and programming department head. This checklist has to be filled by the programmer after developing the program and get the program and the checklist checked and approved by the concerned authority.
Project: Steam turbine rotor Frame: 012
Drawing no: 002
Table 3: Checklist
Sl. No.
Tool Description
Tool path description
Approach checking
Checking Dimension Values
Checked by
1
2
3
166
Inspection time reduction Straight groove and coupling flange holes
Inspection at the straight groove and coupling flange holes using slip gauges takes more time. To avoid this, inspection has to be done by using plug gauges. This would takes less time.
Time reduction for Chip cleaning
Chip cleaning activity is doing by manually and it is time consuming. To avoid this problem chip breaker has to be provided. By providing chip breaker, chip-cleaning time can be reduced.
Estimated time savings after the application of Questioning Technique
Sl.
No.
Setup Operations
Internal Activity time
in min
External Activity time
in min
Remarks
13
Dis-engage both the weight support & engage of
weight support in middle of component
15
14
Machine the steady band areas. Select the depth of cut, cutting speed & feed rate
20
15
Move the steadies in right positions & close them
15
16
Machine 4 disc which are required to align component in this without chattering marks
40
17
Adjust the steady rest by dial gauge in X-Y axis
45
18
The tail stock end side disc can be aligned in X-axis
by using a dial & adjustment screw provided on tailstock
35
19
Work offset taken for probing
70
20
Probe program altered outer diameter runned for X- Y alignment
65
21
X-Y alignment probing
85
22
Measure the same by measuring program and adjust the steady rest until to control the parameter
120
23
Ensure the parameter readings once again that tolerance is within the limit(10-20 microns)
45
24
check the raw part allowance related with the rough turning program
70
25
After rough machining gross check the alignment of component by measuring program
40
26
Disengage the both weight support and engage of weight support in the required position
40
27
Remove the tail stock
5
28
Probe program called and run
55
29
X&Y Alignment done within 0.002micron
80
30
Linear distance cross checked for disc 2-12
65
31
Run out checked after alignment completion within 0.015micron
110
32
Winding the rotor with belt
10
33
Hook the rotor to the crane & check the belt is in balancing for lifting
20
34
Disengage the steady rest Open the jaws and lift the rotor
5
35
Open the jaws and lift the rotor
40
36
Place the rotor on the rotor stand(without removing the belt with crane support)
10
External (Parallel to jaws
removing)
37
Hard jaws removed and soft jaws mounted
35
External (Parallel to positionin g steady
rest)
38
Cleaning
15
External (Parallel to placing
rotor)
39
weight support steady rest position have to be found out so that the weight of the component uniformly distributed from the chuck till tail stock as per the position which has arrived from the
following
40
40
Check the jaws to be opened to enter the component Also check the Z-axis support length where the component rested which machining
5
External (Parallel to loading the componen
t)
-
first disc nearby chuck
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Second & third diameter nearby steady rest
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Fourth one nearby tail stock
Table 4: Estimated cycle time for proposed method
Setup time in min
Actual cutting time
in min
Non-value added time
in min
Total time in min
2280
3258
635
6173
Table 5: Non-value added time (Estimated) in proposed method
Approach time In min
Inspection time
In min
Checking D- values
In min
Chip cleaning time In min
Nil
104
Nil
531
-
-
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Single Minute Exchange of Dies technique
The setup time in manufacturing of steam turbine rotor was
more; to reduce this set up time we had applied Single Minute Exchange of Dies technique.
Setup time reduction by SMED Technique
Table No 6: Streamline the Internal and External activities
Sl.
No.
Setup Operations
Internal Activity time
in min
External Activity time
in min
Remarks
1
cleaning of machine
90
2
Removal of old jaws and fixing new jaws by manually
35
External (Parallel to
cleaning)
3
weight support steady rest position have to be found out so that the weight of the component uniformly distributed from the chuck till tail stock as per the position which has arrived from the
following
40
External (Parallel to cleaning)
4
check the jaws to be opened to enter the component Also check the Z-axis support length
where the component rested which machining
5
External (Parallel to
cleaning)
5
winding the rotor with belt
10
External
(Parallel to cleaning)
6
Hook the rotor to the crane & check the belt is in balancing for lifting
20
7
Load the component in the machine & close the
jaws softly so that the component is approximately in the center of the machine
60
8
Remove the belt from rotor
10
9
Engage the tail stock center. Ensure Z-axis butting
5
10
Engage the weight support on steady rest 1& 2
10
11
Check & correct the run out of component near by check. Tighten the hard jaws fully
125
12
Once again check run out of the component on
same diameter within same limit
30
Contd..
Contd…
Sl.
No.
Setup Operations
Internal Activity time
in min
External Activity time
in min
Remarks
41
Load the component in the machine and close the jaws softly, so that the component is approximately
in the center.
60
42
Remove the belt from the rotor
10
43
Engage the tail stock center. Ensure Z-axis is butting
5
44
Engage the weight support on steady rest 1&2
10
45
Check and correct the run out of the component nearby chuck. Tightened the hard jaws fully
120
46
Once again check run out of component on same diameter within the same limit
30
47
Steady holding on thrust collar outer diameter re- centering done
80
48
Work offset taken for probing
70
49
Probe program altered outer diameter run for X-Y axis alignment
65
50
X-Y alignment probing
85
51
Work offset taken and cross checked by measuring linear dimension
70
52
C-axis done zero
65
TOTAL
2195
185
Table No 7: Results
Operations
Present Method (time in min)
Proposed Method (time in min)
Savings (time in min)
Non value added Activity
Approach Checking
378
Nil
378
Inspection
213
104
109
Checking dimension values
408
Nil
408
Chip cleaning
670
531
139
Set up operations
2280
2140
140
Total
3949
2775
1174
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RESULTS AND CONCLUSIONS
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Critical examination was done for non-value added activities and the non-value added activities time was reduced from 1669 min to 635 min.
SMED Technique was applied to set up operations and set up time was reduced from 2280 min to 2140 min. Following table gives time taken for non-value added activities and set up operations for both present and proposed methods. Hence the cycle time was reduced from 7207 min to 6033 min.
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Results obtained
Savings (estimated) after applying critical examination and single minute exchange of dies (SMED) technique.
Cycle time (present method) = 7207 min Cycle time (proposed method) = 6033 Total saved time in min =1174
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Estimated savings (in terms of cost) to the company
Loss to the company if machining operation is stopped per hour = Rs 6000
Loss per min if machining operation is stopped = Rs 100 Total saved time in min (Estimated) = 1174
Net savings per Rotor (Estimated) = 1174*100 Net savings per Rotor (Estimated) = Rs. 117400
Most of the suggestions given for reducing the cycle time of this steam turbine rotor hold good for many of other types of rotor also. Hence, these suggestions can be implemented for other rotors and cycle time and cost can be reduced to a great extent.
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