Study and Implementation of Total Productive Maintenance in Turbocharger Plant

DOI : 10.17577/IJERTV3IS060941

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Study and Implementation of Total Productive Maintenance in Turbocharger Plant

Chandrashekar G1, Dr. N. V. R. Naidu2

1Student, M. Tech, Department of Industrial Engineering and Management

2Vice Principal,

2Professor & Head, Department of Mechanical Engineering, 2Professor, Department of Industrial Engineering and Management 1,2 M. S. Ramaiah Institute of Technology, Bangalore-560054, India.

Abstract Production System has undergone the major changes in recent years. In the highly competitive environment, to be successful and to achieve world class manufacturing, organizations must possess both effective maintenance and efficient manufacturing strategies. Overall Equipment Effectiveness (OEE) quantifies how well a manufacturing unit performs relative to its designed capacity, during the periods when it is scheduled to run. The data and the behavior of the machines in the cell were analysed and the bottleneck points were identified. The Overall Equipment Effectiveness (OEE) of NU-600 turning centre, MGT-50 turning centre and S-66 milling centre was found to be 60%, 43% and 65% respectively from the data collected in the month of December 2013, January and February 2014.

The techniques of 5S, Poka yoke, Preventive Maintenance and Kaizen which are elements of Total Productive Maintenance are applied effectively on the machines in the cell. The result obtained from the TPM approach showed that the Overall Equipment Effectiveness (OEE) of NU 600 turning centre, MGT 50 turning centre and S 66 milling centre are increased to 71.95%, 69.55% and 75.05% respectively. To sum up, there was an increase in income of Rs.353 per hour from the cell due to effective implementation of TPM technique.

Key Words — Overall Equipment Effectiveness (OEE); Total Productive Maintenance (TPM); Kaizen; Poka yoke; 5S.

  1. INTRODUCTION

    The study is focusing on the machining process of shaft before it is assembled with the turbowheel through auto assembly process. The shafts with two different diameters are machined in the plant that is 50.mm and 60.mm for turbocharger. The tools and products are to be changed frequently due to which the setup time is getting larger.

    There are five machines in the cell and the turbo shaft machining process is described as follows. NU 600 turning centre is performing the operations of Turning, Taper turning and facing on one side of the shaft where turbo wheel is assembled. MGT 50 turning centre is performing Threading on other side where compressor

    wheel is assembled. The end milling and peripheral milling is performed on the S 66 milling centre. The holes on the shaft to place the fasteners are drilled using conventional drilling machine. The burrs on the surface of the shaft are finally removed by deburring machine.

  2. PROBLEM STATEMENT

    The data collected for the 3.months period of December 2013, January 2014 and February 2014 revealed that the Overall Equipment Effectiveness (OEE) value of the machines in the cell are 60%, 43%, 66% which are very low compared to the general manufacturing scenario(OEE

    • 85%). Due to the low OEE, the machines are not effectively utilized. Hence the production is affected and in turn not able to reach the requirements of customer.

      100

      50

      % of OEE

      0

      Dec/13 Jan/14 Feb/14

      Dec/13

      Jan/14

      Feb/14

      NU 600

      59.355

      60.195

      60.555

      MGT-50

      42

      42.395

      45.955

      S-66

      66

      66.5

      66

      Figure 2.1 OEE of the machines from data collected for 3.months

      The bar chart in the figure 2.1 clearly represents the OEE values of the machines for the data collected for 3.months of December 2013, January 2014 and February 2014. The NU-600 turning centre has OEE value of around 60%, MGT-50 turning centre has OEE value of around 43% and S-66 milling centre has OEE value of around 66%. The world class performance of machines has the OEE value of 85% which is far away from any of the machines in the cell. The project focuses on improving the

      OEE of each machine to around 70%, which increases the productivity and improves the delivery time.

      1. Defining the problem

        To study and implement the Total Productive Maintenance (TPM) and 5S techniques in order to improve the Overall Equipment Effectiveness (OEE) of the CNC machining cell present in the turbocharger plant. [1] describes the TPM as a Lean tool to optimize the effectiveness of manufacturing equipment and tooling.

        8000

        Breakdown minutes

        6000

        4000

        2000

        0

        Dec/13

        Jan/14

        Feb/14

        NU-600

        2765

        2489

        1905

        MGT-50

        5975

        6040

        4245

        S-66

        2335

        2185

        1605

        Dec/13 Jan/14 Feb/14

      2. Objectives

        1. To review the literature on TPM related activities and case studies implemented in companies for improving the productivity.

        2. To find out the bottleneck machines in the cell.

        3. To analyse the breakdown data and to identify the critical components.

        4. To form the TPM team to resolve the issues.

        5. To turn around the bottleneck machines into the model machines.

        6. To standardize 5S activities in the cell.

        7. To validate and report the TPM and 5S practices performed.

  3. METHODOLOGY

    1. Data collection

      The data for measuring the performance of the cell was collected for the period of three months from December 2013 to February 2014 for all 3.shifts. The data pertaining to breakdown, setup time, speed loss, minor stoppages, scrap and rework rate were collected and analysed.

      The project focuses on an improving the Overall Equipment Effectiveness (OEE) of the machines as it is the major concern for lower productions and loss of time and money.

      The breakdown details of the three machines for the month of December 2013, January 2014 and February 2014 is as shown in the figure 3.1.

      The total breakdown time in minutes of each machine for three months in total is given below:

      NU-600 turning centre is 7159 minutes. MGT-50 turning centre is 16255.minutes. S-66 milling centre is 6115.minutes.

      Figure 3.1 Break down data from data collected for 3. months

    2. Setup details of 3.machines for a lot of 450 units.

      The total setup time for NU- 600 turning centre, MGT

      • 50 turning centre and S 66 milling centre for machining a lot of 450.units was found to be 185.minutes, 410.minutes and 155. minutes respectively as shown in the figure 3.2. In all the machines second setup was taking more time than first setup.

      500

      Time in minutes

      400

      300

      200

      100

      89

      225

      95

      2nd setup

      66

      85

      S – 66

      MGT -50

      NU – 600

      0

      1st setup

      185

      Total

      155

      410

      175

      Figure 3.2 Setup details for the period of 3.months

      Table 3.1 represents the parameters of OEE which are critical and need to be focused on ach machine in order to increase the Effectiveness. The parameters which are represented in colored blocks are to be focused in order to bring the operations to the normal conditions.

      Table 3.1 Comparison of critical parameters of 3.machines

      Machine

      Parameters to be focused (%)

      Availabilit

      y

      Performanc

      e

      Quality

      OEE

      NU 600

      84

      75

      96

      60

      MGT- 50

      66

      66

      95

      43

      S 66

      86

      77

      96

      65

    3. System Analysis through Simulation

      Figure 3.3 Utilisation factor of different machines in the cell through simulation

      From the simulation Analysis of the system as shown in the figure 3.3, it is clear that the MGT 50 turning centre is the bottleneck because of its high cycle time and breakdowns. There is a queue of 2.parts on an average all the time before MGT 50 turning centre and waiting time is around 7.minutes/part. We can conclude that MGT 50 turning centre needs more focus and necessary actions to be taken to bring it to the normal conditions.

    4. Capacity and existing condition of cell

      Figure 3.4 Process parameters of all machines in the cell

      As it can be observed in the flow chart in figure 3.4, the MGT 50 turning centre is in the middle of the cell. The parts processed from the NU_ 600 turning centre were piled up before MGT- 50 as the cycle time of NU- 600 is 3.minutes and MGT 50 is 4.minutes. Due to slow cycle rate and breakdowns, the parts are not sufficiently passed on to the next centre for processing and therefore causing the stoppage of line. Thus, hindering the production and reduces the effectiveness and efficiency of the line.

    5. Implementation phase

      Figure 3.5 Cause and Effect Diagram for low OEE of the machines

      The figure 3.5 shows how the 4M Man, Machine, Material and Method are affecting the OEE of the machine. The causes which are highlighted in the diagram are found to be major causes from the analysis. The cleaning kit was effectively used by each team and necessary cleaning actions were taken to efficiently perform 5S activities and to identify the abnormalities in and around the machines. After the cleaning was completely performed on the machines, the abnormalities identified and it was recorded in a pareto for an observation and an analysis. It is observed that around 80% of occurrences of abnormalities are due to Coolant leakage, Chipping problems, Loosed fasteners and screws, unwanted materials and dirt. [2] The primary goal of the technique is to determine the root cause of a defect or problem.

      The checklist which involved daily activities such as greasing chuck, checking the oil level, cleaning AC filter etc. was provided so the machine was maintained after the cleaning activity was performed and all the spare parts were replaced and repaired. Few Kaizen approaches were also performed in and around the cell. In Japan, the concept of Kaizen is so deeply engrained in the minds of both managers and workers that they often do not even realize they are thinking Kaizen as a customer-driven strategy for improvement [3].

      1. To eliminate the extra setting by providing a rigid clamping in the first setup

        The idea was incorporated as the processing time was more due to the second setting taking long time due to low parameters. A revised process plan was made for single setup with holding at the bigger ends of the parts so that the pressure applied can be high and the cutting area could be increased. The second setup causes the higher cycle time due to low parameters specified in the process. The idea was to eliminate the second setup as it could be done in the first setup itself with some clamping alterations. The setting time is reduced from 410.minutes to 90.minutes. The above clamping modification helped in decreasing the cycle time from an average of 4 minutes to around 3.3minutes.

    6. Quality Approach

      The quality aspect of the machine had no problems as the quality was maintained at 95%. To improve the quality level, the TPM team decided to implement Poka yoke on all the three .machines of interest which would fool proof the process. The team implemented poka yoke on each centres which is discussed in common to all the three machines.

      Poka yoke – 1

      Plate provided

      Figure 3.6 Poka yoke modifications

      Parts were placed with wrong orientation, which caused the parts to fell down from the storage space and become scraped. In order to avoid this, the TPM team provided the side plate with the fixtures is as shown in the figure 3.6 which blocks the space if the parts are placed wrongly. It avoids the slipping of parts placed in the space provided.

      Poka yoke 2

      Pre machined parts length is not controlled, which resulted in tool breakage while turning in MGT – 50 turning centre. This problem was occurred 6.times in 3.months. In order to avoid the tool breakage, the height guage is placed next to the machine and was made part of the inspection, where the operators had to inspect the piece and if oversize parts are there, they must be machined to required size and then turn it.

    7. Improving OEE of NU 600 turning centre and S- 66 milling centre

      As we incorporated the tagging system for MGT- 50 machine, the tags were hanged to NU 600 turning centre and S- 66 milling centre similarly. The white tags and red tags were hanged based on the normal techniques as done in the MGT- 50 turning centre. All the data was recorded and then analysed, action was taken to see that it was rectified. The missing parts were replaced and the faulty parts were repaired based on the tagging system. All the steps are followed similar to that followed on MGT- 50 turning centre.

    8. Design modifications in NU 600 turning centre Quick Change Jaw Concept Design

    The traditional jaws were used initially and the replacement time of the jaw is considerably high. Due to the high number of part count, also trial and error alignment of bolts and tightening and loosening the bolt time was more. To avoid the trial and errors and to eliminate the whole chuck replacement theory the new quick change jaws were designed. And the jaws were designed to accommodate both the products on to the single chuck.

    Earlier the operator had load two different chucks to run both products due to the product geometry variation and now the larger existing chuck is used and only the top soft jaws are going to be changed. The figure 3.7 shows the schematic arrangement of changeover process on turning centers. The special jaws arrangement is shown in figure

    3.8 for individual products which were designed to reduce the Change Over Time.

    Figure 3.7 Quick change jaw Concept

    Figure 3.8 Quick change jaw Process

  4. RESULTS AND DISCUSSION

    The results obtained by implementing the TPM methods are explained step wise, the individual improvements obtained are shown on the three parameters separately.

    1. Availability results

      The major problems of coolant leakage and the chip fall out due to which hydraulic motor was failing regularly and the lead screw getting damaged frequently from the chips accumulation was avoided. The above parts are replaced immediately which reduced the breakdown by 3.hours per day. The breakdown details after the implementation of TPM techniques are as shown in the figure 4.1.

      Time in minutes

      1700

      1600

      1500

      1400

      1300

      1635

      MGT-50

      NU-600

      April – May 2014

      1200

      1595

      1375

      S-66

      Figure 4.1 Breakdown details of machines after TPM implementation

      Total available production time per month = 410* 25 = 30,750 minutes. (Considering 25.days working and 410.minutes per shift excluding the breaks)

      Breakdown per month on an average is given in the table 4.1.

      Machine

      Before TPM

      After TPM

      Time in minutes

      %

      breakdo wn

      Time in minutes

      %

      breakdo wn

      NU 600

      2500

      8.15

      1595

      5.15

      MGT 50

      5500

      17.85

      1635

      5.35

      S – 66

      1900

      6.15

      1375

      4.45

      Table 4.1 Breakdown time in minutes of 3.machines

      Note: % breakdown is calculated by, (% breakdown) =

      1. Setup time reduction for a lot of 450units.

        Time in minutes

        500

        400

        300

        200

        100

        90

        MGT – 50

        After TPM

        Before TPM

        0

        410

        Figure 4.2 CNC setup details of machine for lot of 450.units

        Figure 4.2 shows that the reduction in the setup time after the implementation of the TPM techniques. Earlier there was a long second setup time due to part dimension changes and increases the process time because of insufficient cutting area and pressure. The modifications in the clamping process and fixtures were made because of which the setup was combined. As a result, the availability (%) of the MGT 50 turning centre, NU 600 turning centre and the S 66 milling centre were increased as in table 4.2.

        Table 4.2 Comparison of % Availability for 3.machines

        Machine

        Before TPM

        After TPM

        % Availability

        % Availability

        NU 600

        83

        86

        MGT 50

        66

        88

        S – 66

        83

        88

    2. Performance Results

      The improvements and results of modifications are shown below.

      1. The balancing of the man and machine working time was achieved by proper training to operators.

      2. The operator movements to pick and place the tools were reduced by providing the shadow board to each machine and in turn reduce the cycle time.

      3. The combining of tools which resulted in saving of 1.minute between each parts and the cycle time was reduced from 4.minutes to 3.minutes.

        Table 4.3 Comparison of % Performance before and after implementation of TPM

        Machine

        Before TPM

        After TPM

        % Performance

        % Performance

        NU 600

        75

        84

        MGT 50

        66

        90

        S – 66

        77

        91

    3. Quality Results

      The machines were producing quality products with the rejection rate of 5%. The quality level did not demand any improvement. However, it was necessary to sustain the current level of quality. Further, the team decided to monitor current level effectiveness with some additional fool proof methods which are already discussed earlier.

    4. OEE improvement

      Due to the systematic approach in implementation of TPM, the OEE of the bottle neck machine MGT 50 turning centre, NU 600 turning centre and S 66 milling centre are increased to 69.55%, 71.95% and 75.075% respectively. The chart of the OEE (%) values before and after implementation of TPM techniques is as shown in the figure 4.3.

      NU – 600

      MGT – 50

      S – 66

      OEE (%) Before TPM

      60

      43

      65

      OEE (%) After TPM

      72

      70

      75

      80

      OEE in (%)

      70

      60

      50

      40

      30

      20

      10

      0

      Figure 4.3 OEE (%) before and after implementation of TPM techniques

    5. Cost aspects

    The income to the company relative to the increase in the OEE of the machines in the cell is as shown in the table

    4.4. Total increase in the income of Rs. 2825/ shift was achieved due to the effective implementation of TPM techniques in and around the cell.

    Table 4.4 Comparison of income from the cell before and after TPM implementation

    Machines

    Income from the cell in Rs./shift

    Increase in income

    in Rs./shift

    Before TPM implementation

    After TPM implementation

    NU 600

    2700

    3250

    550

    MGT

    50

    2900

    4725

    1825

    S 66

    2925

    3375

    450

    Total

    8525

    11350

    2825

  5. CONCLUSION

In general the focus of almost all the industries is on downtime losses especially breakdowns. Many losses are not targeted enough today i.e, planned downtime, cycle time losses and minor stoppages. It is beneficial to change the focus and use a comprehensive model of losses. In order to utilize the OEE measure effectively, it must be convincing and credible to production management. In order to achieve the target performance, efficient maintenance was installed in the workplace, Autonomous maintenance teams were developed and the better communication with team work was promoted. Efficient data recording system was installed in order to provide the upto date and accurate information to the management. The increase in an income of Rs. 353 per hour was achieved because of the effective implementation of the TPM and the 5S techniques in the plant.

AKNOWLEDGMENT

The author wishes to express his gratitude towards Mr. Nittala Srinivas and Mr. Venkata Ravisankar, XYZ organisation, Bangalore for their constant help and encouragement.

REFERENCES

  1. Dave Hoyte , Total Productive Maintenance Overview, Available from http://fisher.osu.edu/~ward_1/BM840/tpm.ppt, 2005.

  2. Taiichi Ohno; foreword by Norman, Toyota production system: beyond large-scale production., Portland, Or: Productivity Press., 1988, ISBN 0-915299-14-3.

  3. Imai,M., Kaizen :The key to Japans competitive success,

McGraw Hill, 1986,USA,pp.xxix

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